BIOLIS 24I CHEMISTRY ANALYZER PDF

Contributing to the medical treatment and health of people worldwide through opening up desktop clinical examination medical equipment market and always developing products from the perspective of customers. Tokyo Boeki Medisys Inc. With a sales network stretching across more than 80 countries worldwide, the company has already sold more than 7, units, holding top share globally among desktop blood analyzers. In April , the company became the successor to the sales division of the group company Tokyo Boeki Machinery Ltd. Engineers with advanced expert knowledge, sales-service engineers who directly hear the concerns of customers, and all other employees work together to contribute to medical care and the health of people around the world through the development and sales of products equipped with the latest technology.

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Sample control. If the encoder difference value appears correct, Reinstall or upgrade software software bug or damaged database is the cause. If the encoder difference value appears correct, Reinstall or Update software software bug or damaged database is the cause.

Home sensor trouble manual function screen. It the sensor light is or cable cut-off interrupted, the indicator turns red from blue. Replace control PCB. Rotation Outside Motor Busy motor stop signal. Motor is out of control, because of over load. Examine the motor smooth rotation while the power is If motor does not rotate smoothly, perform the unit Sens.

Erro The sensor pin could run over the stop position off. If the encoder difference value appears strange, the Examine the encoder values at the encoder screen. If the encoder values appear wrong, replace the Wash-center The encoder difference value is far from the theoretical encoder is in trouble or the stepping motor is out of stepping motor with the encoder and then perform the one.

TimeOut STM fails to move from the washing position to the The home sensor is in trouble or some cable is broken Confirm if STM-R home sensor works normally by If the sensor does not work, replace the home sensor or outer sample position within the defined time examining the sensor function on the screen in the the sensor cable. Confirm if motor rotates smoothly by hand while the If motor does not rotate smoothly, perform the unit power is turned off. Replace 5-phase pulse motor driver as a trail 5-phase pulse motor driver replacement.

Erro position The sensor pin could be above the home screen of manual operation screen. Confirm if the motor rotates smoothly by hand while If motor does not rotate smoothly, perform the unit the power is turned off. If the encoder presents incorrect values, the encoder has Confirm the encoder difference value for STM on the If encoder data is found wrong, the encoder has trouble Wash-center the actual encoder value went far from the theoretical trouble or the motor is out of control.

Cell 5-phase pulse motor driver has trouble. Confirm if STM up position home sensor works If home sensor does not work, replace sensor or sensor Sens. Erro position The home sensor pin could be above the home normally on the sensor screen in the manual function cable.

Confirm if motor rotates smoothly by hand while the If motor does not rotate smoothly, perform the unit power is turned off adjustment including the timing belt, the shielding plate position and the bearing rotation STM-R Not STM does not stop in the correct outer sample If the encoder presents incorrect values, the encoder has Confirm the encoder difference value for STM on the If encoder data is found wrong, the encoder has trouble Outside Bo position.

The encoder difference value went far from trouble or the motor is out of control. Replace the motor the theoretical value. Motor is out of control because of overload. Confirm if the motor rotates smoothly by hand while If motor does not rotate smoothly, perform the unit the power is tuned off. Replace 5-phase pulse motor driver. Software bug or broken file. Confirm if motor rotates smoothly by hand while the If motor does not rotate smoothly, perform the unit power is turned off adjustment including the timing belt, the shielding plate position and the bearing rotation STM-R Not STM does not stop in the correct inner sample If the encoder presents incorrect values, the encoder has Confirm the encoder difference value for STM on the If encoder data is found wrong, the encoder has trouble Inside Bot position.

Replace the motor the theoretical value including the encoder and then perform the unit position readjustment. Cell Motor Busy motor. Home sensor has trouble or cable is broken. Erro Not at up home position normally on the sensor screen in the manual function cable. Confirm if motor rotates smoothly by hand while the If motor does not rotate smoothly, perform the unit power is turned off adjustment including the timing belt, the shielding plate position and the bearing rotation STM-R Not STM does not stop in the correct dilution position.

If the encoder presents incorrect values, the encoder has Confirm the encoder difference value for STM on the If encoder data is found wrong, the encoder has trouble Dilution P The encoder difference value went far from the trouble or the motor is out of control. Replace the motor theoretical value including the encoder and then perform the unit position readjustment.

Wash Motor Busy motor. Replace 5-phase pulse motor driver 5-phase pulse motor driver replacement. Confirm if motor rotates smoothly by hand while the If motor does not rotate smoothly, perform the unit power is turned off adjustment including the timing belt, the shielding plate position and the bearing rotation STM-R Not STM does not stop in the correct outer sample If the encoder presents incorrect values, the encoder has Confirm the encoder difference value for STM on the If encoder data is found wrong, the encoder has trouble Cell pos.

Replace the motor with the theoretical value. Confirm if motor rotates smoothly by hand while the If motor does not rotate smoothly, perform the unit power is turned off adjustment including the timing belt, the shielding plate position and the bearing rotation TimeOut STM failed to detect the home sensor signals within the Home sensor has trouble or cable is broken.

Confirm if STM up position home sensor works If home sensor does not work, replace sensor or sensor defined time. Confirm if motor rotates smoothly by hand while the If motor does not rotate smoothly, perform the unit power is turned off adjustment including the timing belt, the shielding plate position and the bearing rotation Other Safety STM-R Software has failed to detect signals for stopping the UCNT-1PCB has trouble.

Motion Motor Busy motor. Confirm if STM up position home sensor works If the home sensor does not work, replace sensor or Sens. Erro position The home sensor pin could be above the home normally on the sensor screen in the manual function sensor cable. Confirm if motor rotates smoothly by hand while the If motor does not rotate smoothly, perform the unit power is turned off adjustment including the timing belt, the shielding plate position and the bearing rotation STM-R Not STM does not stop in the correct outer sample If the encoder presents incorrect values, the encoder Confirm the encoder different value for STM on the If the encoder presents incorrect values, the encoder has Outside Bo position.

The encoder difference value went far from has trouble or the motor is out of control. Replace the the theoretical value motor with encoder attached to it. Perform the unit position adjustment. Poor contact of the encoder extension cable. Replace extension cable Replace extension cable. The encoder difference value went far from or the motor is out of control.

If the encoder value is correct, software bug or the Software re-installation or updated software installation corrupted system program file is the factor. If a new part is not Open because the ISE door is left open.

The If the encoder value is correct, the encoder has trouble Confirm the encoder different value for STM on the If the encoder presents incorrect values, the encoder has ISE pos. Replace the value motor with encoder attached to it. If the encoder value is correct, the encoder has trouble Confirm the encoder different value for STM on the If the encoder presents incorrect values, the encoder has Cell pos. The encoder difference value went far from the or the motor is out of control. Replace the theoretical value motor with encoder attached to it.

TimeOut STM failed to detect the home sensor signals within the Home sensor has trouble or cable is broken. Busy motor. Erro incorrect position.

The home sensor pin could be normally on the sensor screen in the manual function sensor cable. Confirm if motor rotates smoothly by hand while the If motor does not rotate smoothly, perform the unit power is turned off adjustment including the timing belt, the shielding plate position and the bearing rotation STM-R, STM stops in an incorrect sample position.

The If the encoder presents incorrect values, the encoder Confirm the encoder different value for STM on the If the encoder presents incorrect values, the encoder has Sample pos.

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